EXPERIMENTAL STUDY ON MECHANICAL BEHAVIOR OF EXISTING UN-CARBONATED CONCRETE
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摘要: 根据对已使用了10、20、40年的既有未碳化混凝土所进行的单轴受压试验结果和测得的24条应力-应变全过程曲线,发现其延性比、峰值应变、极限应变和弹性模量与同强度的新混凝土(龄期28d)相比,均有不同程度的下降,总结了它们随使用年限的变化规律,指出对既有钢筋混凝土结构构件继续使用时应考虑这些不利因素的影响。Abstract: This paper describes a series of tests carried out on the uniaxial compression of ex isting un-carbonated concrete that had been in service for 10, 20 and 40 years, respectively, and 24 complete stress-strain curves in total were obtained.Compared with fresh concrete of the same strength ( 28 days of curing period), the behavior parameters in terms of ductility ratio, peak strain, ultimate strain and elastic modulus were found to decline to different degrees and the chang ing laws of these parameters with the increase of service life were generalized based on the test results. It is therefore recommended that the adverse effects of these parameters should be taken into account if members are planned to be used further.
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Key words:
- ex isting concrete /
- stress-strain curve /
- service life /
- ductility ratio /
- elastic modulus
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过镇海.钢筋混凝土原理.北京:清华大学出版社,1999 [2] 过镇海,张秀琴,张达成,等.混凝土应力-应变全曲线的试验研究.建筑结构学报,1982(1) [3] 过镇海.混凝土的强度和变形试验基础和本构关系.北京:清华大学出版社,1997
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